Ultimaker 2: Difference between revisions
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(→Machine Log: Print Bed & Carbon Fiber Plate notes) |
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|February 28, 2018 | |||
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* Using a feeler gauge & Machine Shop straight edge, determine that the center of the plate '''is high by more than 0.2mm'''. | |||
* HOWEVER, the other side has a different high/low spots pattern, that is out by '''less than 0.1mm'''. (More than 0.06mm, and less than 0.1mm) | |||
* So able to get the Carbon Fiber Plate working to print on, by ONLY using the '''one good side'''. | |||
** See the Known Issues and Fixes section, about the loose wood under-structure that holds the build plate. | |||
|Allen | |||
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|February 20, 2018 | |||
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* 300mm X 200mm X 3mm Carbon Fiber Plate purchase for printing on is HIGH in the Center. | |||
* After installing (without cutting) takes HOURS to get the bed leveled. (Front left spring can't go up more. Back right level screw seems jammed.) | |||
* Once leveled, CAN finally print on entire print bed, but high center has print in that area toooo close, in a way that will always rip blue tape when taking the print off. | |||
|Allen | |||
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|February 8, 2018 | |February 8, 2018 |
Revision as of 05:58, 1 March 2018
This page documents Ultimaker #2 (Fawkes) [A phoenix from the ashes]
Printer lives on the third shelf of the 3D printer tower, next to the Type A.
Status
Old/Brittle Filament ... do NOT leave this filament loaded when done printing!
"Canada 150" Red PLA (from Filaments.ca)
- Last known good settings: (05-Dec-2017, Pastel Yellow PLA) 220°, 138% flow, print @ 50mm/s, travel @ 150mm/s, 0.4 mm nozzle size, 2.85mm filament size.
- note: the reason the flow is pumped-up is because the print-head is misaligned and causing drag on the filament. I suspect you could even up the flow and the speed and get decent (but still crappy) prints. If you want to print slower for higher precision you may need to reduce the flow (but <110% flow at any speed will cause under-extrusion)
- Operational ... it can be Problematic
- Using a Brim to hold parts to the Print Bed is strongly recommended.
- Bed was leveled, but wood support structure is loose! (See Known Issues and Fixes section about that.)
- If head too close & extruder starts clicking, that can cause filament feed problems.
- Set X-axis to about 102% of Y-axis Scale to get square/round prints. (Pink 20mm X/Y/Z cube beside printer.)
- PLA ONLY! (to prevent nozzle contamination)
- Cura 15 Settings here
- http://octopi2.hacklab.to/
Known Issues and Fixes
- IMPORTANT: OctoPrint will disconnect from Ultimaker 2 if Ultimaker 1 is powered on. If you want to print on both (or will want to eventually), power both on before starting to print on Ultimaker 2
- The wood support structure that holds the printbed is loose! At least on 1 side, a partial disassembly may be needed, to reverse which side the bolt heads are on, and which side the nuts are on.
- FOR NOW: Grab both sides of the front wood structure (just outside the bed level screws), then gently move one side up, while the other moves down, to get the bed level. (Bed seems to stay level for printing once ajusted.)
- The flatness of the used side of the 3mm Carbon Fiber Plate is out by LESS than 0.1mm ... so large prints should again be possible on this printer.
- If needed, manually adjust the Z-axis for the first layer until the filament is being laid down flat (not rounded).
- Turn the threaded rod clockwise to bring the head closer to the print bed, and counter-clockwise to move the head further away.
- This printer is in fairly rough shape mechanically. This causes the most problems with prints that have thin filled walls.
- Printing slower and at a higher flow rate can help with getting acceptable print quality.
- 220°, 110% flow, print @ 30mm/s (1/2 speed), travel @ 60mm/s (also 1/2 speed), 0.4 mm nozzle size, 2.85mm filament size are the safe settings for this printer.
- Excellent results have been reported using 220° & 135% flow. However, anything above 110% flow makes head jams more likely. (Some filament reels will work @ higher flow, while others constantly jam.) Thus reducing both print speeds is sometimes a better answer than increasing the % flow above 110%.
- Printing slower and at a higher flow rate can help with getting acceptable print quality.
- Filament Loading Problem: the printhead is all misaligned, specifically the PEEK peice (light brown in colour) to the teflon coupler (white in colour) above it. Trying to push filament through there to the nozzle is difficult. Try to make a long and sharp point on the end of the filament, the longer the better, so it gives plenty of space to wiggle around in when shoving it in. You can see through the tube going into the top of the teflon piece, so use that to judge how far down the filament has gone. It probably helps to have the nozzle hot, but don't keep the nozzle hot with no filament inside because it is likely to burn plastic/dust inside the nozzle and cause friction issues.
Features
- Ultimaker Original with extruder drive upgrade
- Built from an incomplete kit and a bunch of parts are 3D printed
- 210 x 210 x 205 mm print volume (Carbon Fiber Plate for printing on is only 200mm wide.)
- 2.85mm filament
- Absolute max temperature: 250 C
- It is managed and accessible from the web GUI: http://octopi2.hacklab.to/
Machine Log
Date | Notes | Entry By |
---|---|---|
February 28, 2018 |
|
Allen |
February 20, 2018 |
|
Allen |
February 8, 2018 |
|
Allen |
October 19, 2017 | Replaced broken (physically split) Power Jack. | atrain |
October 12, 2017 |
|
Allen |
July 13, 2017 |
|
Allen |
June 23, 2017 |
|
Allen |
Jun 8-9, 2017 | Extruder DIED! (Plate that the Tension Arm screws into is cracked/broken.)
|
Allen |
Jun 7, 2017 | Lubricate the Z screw using Superlube Synthetic Grease. | Allen |
June 6, 2017 | Replaced the brass nozzle with a brand new one. Still underextruding though... whole head needs disassembly and new parts I think. Got a decent print at 40 mm/s, 220 deg, 110% flow, and nozzle size at 0.3mm | rana |
June 1, 2017 |
Suspected the Translucent Yellow filament was aggravating the problems w/ this printer ... so changed the filament to a Pastel Pink roll, which is like the other rolls that have worked well. Now printer works fine @ 220°C & 110% Flow. |
Allen |
May 24, 2017 |
|
Allen |
April 28, 2017 | Tightened all the frame screws. Unwittingly tightened the tensioner screw on the rails (the middle screw of those plastic pieces on the frame) and the head would not move. Loosened them and head moves well now.
The plastic connector for the printhead fan was coming in between the head and the orange rail holder, preventing homing. Secured that wire using a zip tie. |
Rana |
April 26, 2017 | Filament was not extruding, took out the Bowden tube in the printhead and put it back in, it went several mm further in. Extruding fine now. | Rana |
April 19-20, 2017 |
|
Allen |
April 5, 2017 | Lubricate Y-Axis rods using NCR Silicone Fluid. Hardened/old lubricant on the Y-axis rods also removed by doing this. Using 30AWG wire to try cleaning print head. (Some dirt came out. Filament still curls towards head.) | Allen |
March 9, 2017 | The Print Head Fan Duct was touching the build plate before the front/right corner was down enough to be level. Used a fine file to trim the underside of this 3D printed part, so this now stays just slightly above the build plate at all times. | Allen |
March 1, 2017 | X axis just stopped working mid-print again. Re-seated x axis stepper board again, and this time used Kapton Tape to secure all the the stepper board DIPs in place. | Allen |
February 28, 2017 | Lubricate X-Axis rods using NCR Silicone Fluid. X-Axis now moves back & forth smoothly. (Left side of belt no longer bends sideways @ the stepper motor.) Hardened/old lubricant on the X-axis rods also removed by doing this. | Allen |
February 21, 2017 | Igor helped to locate & fix bad driver board (DIP socket) connections for the X axis stepper motor. Removed broken PLA from feeding tube (yet again). The working PLA reel from Ultimaker 1 was moved to this unit. | Allen |
Mid-2016 | Re-printed extruder drive tensioner in ABS on Ultimaker 1, replaced Bowden tube coupler springs. Snipped 1cm off the tube ends to give couplers fresh surface to hold on to. | Igor |
September 26, 2015 | Removed overly-brittle, broken PLA from the feeding tube. Machine back in working order with new PLA. PLA can become stale and brittle due to moisture absorption. | Justin |
July 28, 2013 | Found new Arduino mega and installed marlin firmware via CURA. Checked all axis movements, checked thermocouple via external temperature sensors and finalized hot-end. Installed build platform. Removed raspberry pi. | Norm |
July 27, 2013 | Cemented thermocouple into tube, fit tube into hot end. Attempted firmware uploads using Cura (failed) and Xloader (succeeded) | Norm |
June 23, 2013 | Machined remaining parts and assembled feeder, mounted and tested (dry run without power, tensioner only). Attached flying lead ends of thermocouple onto thermocouple amp. |
Norm |
June 22, 2013 | Printed out and assembled most of the feeder, lubricated gantry. | Norm |
June 18, 2013 | Printed out parts for feeder | Norm |
June 10, 2013 | Stripped apart old filament feeder and began building new feeder which uses the hobbed pulley. Parts on order, machined other parts. | Norm |
June 8, 2013 | Rebuilt hot-end, rebuilt gantry components, mounted entire gantry, roughly aligned belts, verified general mechanical functions! Finished mounts for build platform (cutting build platform and mounting to be completed). |
Norm |
May 29, 2013 | Boden tube, V2 hot end components, and belts arrived. | Norm |
May 16, 2013 | Ordered Boden tube and V2 hot end components (the feeder upgrade can be printed for cheap). Belts ordered for Ultimaker 1 (when they are needed for replacement). (~$138) | Norm |
May 15, 2013 | Printed Z home switch adjustment block and holder. Designed and printed parts for new build platform system. |
Norm |
April 29, 2013 | Printed fourth X/Y bushing block and Raspberry Pi bracket | Norm |
April 27, 2013 | Assembled 3/4 X/Y bushing blocks, 4th print failed mid-print. | Norm |
April 24, 2013 | Unmounted dual extruder.
Stripped out X/Y gantry parts for rebuild (X/Y blocks broken). |
Norm |
April 22, 2013 | Reorganized shelf to accommodate the Ultimaker, organized materials and supplies. | Norm |
Parts and Supplies Wish List
- www.aliexpress.com/item/A-Funssor-4pcs-Ultimaker-Original-UM2-Plus-Printhead-Corner-Thumbscrews-M3-60-70-m-Print-Head/32838283972.html
- Strongly suggest shipped by ePacket (becomes XpressPost in Canada.)
- Thumb Screw spec's: github.com/Ultimaker/Ultimaker-Original-Plus/tree/master/1680%20Print%20Head%20Thumb%20screw%2062mm